+Advanced Search

Investigation of the Wind-induced Responses of a Tower 838 m High Based on a Multi-degree-of Freedom Aero-elastic Model Wind Tunnel Test
Author:
  • Article
  • | |
  • Metrics
  • |
  • Reference
  • |
  • Related
  • |
  • Cited by
  • |
    Abstract:

    In order to investigate the wind-induced responses of a tower 838 meters high under the designed wind speed, multi-degree-of freedom aero-elastic model wind tunnel tests were carried out. It was found that the first-order and the second-order frequency inaccuracy of the model, which was measured from the free vibration test, were less than 1% and 28%, respectively, the first-order damping ratio was about 2%, and the translational vibration mode shape was consistent with the actual structure. Wind tunnel test result has shown that the maximum wind-induced dynamic displacement is 0.89m, which is in the standard allowable range. But the wind-induced acceleration of 10 years', 50 years' and 100 years' return period exceeds the specification threshold with the amplitude of 16%, 23%, 29%, respectively. What's more, the lateral response increases remarkably by first order vortex induced vibration,in which the contribution of aerodynamic damping is close to 37%.And in order to ensure acceleration response under one hundred years' wind speed in the allowable range, the structural damping ratio must be larger than 2.9%.

    Reference
    Related
    Cited by
Article Metrics
  • PDF:
  • HTML:
  • Abstract:
  • Cited by:
Get Citation
History
  • Online: January 27,2015